Figure 1. This is the way the differential pressure controllers and valves were meant to be linked.
Using temperature control would have been difficult. Phase change is occurring throughout the heat integration circuit on both the reactor feed and reactor effluent side. Small measured temperature differences would represent large shifts in duty.
The control objective was to have equal duties in each leg of the heat integration system. Process needs made the duty of Reboiler One approximately 1.5 times that of Reboiler Two. Optimal operation required balancing the heat loads to get equal inlet temperatures upstream. The ability to set different values for the two DPC loops was supposed to allow for bias control on the entire system.
Charitably, this would be described as a difficult system to control. Each combined temperature-control-valve/reboiler system is being treated as a head flow meter element to adjust a second control valve. The bias between the differential pressure readings on both flow loops would require constant re-setting for accurate control. Due to the pressure balance, small changes in valves TV47 and TV53 have a large impact on the flow split. For example, a change of 3.6% of system pressure drop (or 2 psi) across TV47 would change the amount of flow through that loop by almost 21%. To add an extra level of complexity, the larger temperature control valve had been installed on the loop for the smaller duty.
Difficult to control as it was, this arrangement might have sufficed. In practice, though, the control system continuously hunted. Operators were constantly intervening to reset valve position and flow rates. The system performed much worse than anticipated.
A careful check of the documentation was illuminating. The process flow diagrams, piping and instrumentation diagrams, isometric drawings, and control computer documentation didn’t agree with each other. They contained different configurations of the control links between the flow loops for DPC65/66 and PV65/66. Field verification revealed that the unit was actually configured as shown in Figure 2.